Properly declare that the g10 is booting from NAND and define its
correct (larger than on other devices-) boot_pages_size, to prevent
the kernel from constantly falling over missing OOB error correction
for the bootloader.
This patch prevents a constant slew of (bogus) read errors reported
by the kernel and keeping the CPU busy and fixes:
blk_update_request: I/O error, dev mtdblock0, sector 0 op 0x0:(READ) flags 0x80700 phys_seg 4 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 8 op 0x0:(READ) flags 0x80700 phys_seg 3 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 16 op 0x0:(READ) flags 0x80700 phys_seg 2 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 24 op 0x0:(READ) flags 0x80700 phys_seg 1 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 0 op 0x0:(READ) flags 0x0 phys_seg 1 prio class 0
Buffer I/O error on dev mtdblock0, logical block 0, async page read
blk_update_request: I/O error, dev mtdblock0, sector 32 op 0x0:(READ) flags 0x80700 phys_seg 8 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 40 op 0x0:(READ) flags 0x80700 phys_seg 7 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 48 op 0x0:(READ) flags 0x80700 phys_seg 6 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 56 op 0x0:(READ) flags 0x80700 phys_seg 5 prio class 0
blk_update_request: I/O error, dev mtdblock0, sector 64 op 0x0:(READ) flags 0x80700 phys_seg 4 prio class 0
Buffer I/O error on dev mtdblock0, logical block 1, async page read
Buffer I/O error on dev mtdblock1, logical block 0, async page read
Buffer I/O error on dev mtdblock1, logical block 1, async page read
Buffer I/O error on dev mtdblock2, logical block 0, async page read
Buffer I/O error on dev mtdblock2, logical block 1, async page read
Buffer I/O error on dev mtdblock3, logical block 0, async page read
Buffer I/O error on dev mtdblock3, logical block 0, async page read
Buffer I/O error on dev mtdblock4, logical block 0, async page read
Buffer I/O error on dev mtdblock4, logical block 1, async page read
Suggested-by: Ansuel Smith <ansuelsmth@gmail.com>
Signed-off-by: Stefan Lippers-Hollmann <s.l-h@gmx.de>
RT-AC57U and RT-AC1200GU are the same models sold in different countries.
The purpose of this commit is to allow users to easily find the
corresponding firmware through the model number on the device label.
More specifications: 14e0e4f138 ("ramips: add support for ASUS RT-AC57U")
Signed-off-by: Shiji Yang <yangshiji66@qq.com>
[reword commit title/message]
Signed-off-by: Sungbo Eo <mans0n@gorani.run>
ipTIME T5004 is a 5-port Gigabit Ethernet router, based on MediaTek MT7621A.
Specifications:
* SoC: MT7621AT
* RAM: 128 MiB
* Flash: NAND 128 MiB
* Ethernet: 5x 1GbE
* Switch: SoC built-in
* UART: J4 (57600 baud)
* Pinout: [3V3] (TXD) (RXD) (GND)
Installation via web interface:
1. Flash **initramfs** image through the stock web interface.
2. Boot into OpenWrt and perform sysupgrade with sysupgrade image.
Revert to stock firmware via recovery mode:
1. Press reset button, power up the device, wait >15s for CPU LED
to stop blinking.
2. Upload stock image to TFTP server at 192.168.0.1.
Signed-off-by: Sungbo Eo <mans0n@gorani.run>
* Add support for Sophos SG/XG-115 r1, r2 with/without wireless
* Add support for Sophos SG/XG-125 r1, r2 with/without wireless
* Add wireless support for SG/XG-105
Signed-off-by: Raylynn Knight <rayknight@me.com>
On startup the USB of QCA9531 board can't be initialized successfully.
lsusb result as below:
root@OpenWrt:~# lsusb unable to initialize libusb: -99
This is because usb-phy-analog is not added to reset list.
Signed-off-by: Jinfan Lei <153869379@qq.com>
(added linebreaks and small little changes to the commit message)
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
mtd: spi-nor: locking support for MX25L6405D
Macronix MX25L6405D supports locking with four block-protection bits.
Currently, the driver only sets three bits. If the bootloader does not
sustain the flash chip in an unlocked state, the flash might be
non-writeable. Add the corresponding flag to enable locking support with
four bits in the status register.
mtd: spi-nor: disable 16-bit-sr for macronix
Macronix flash chips seem to consist of only one status register.
These chips will not work with the "16-bit Write Status (01h) Command".
Disable SNOR_F_HAS_16BIT_SR for all Macronix chips.
Refreshed:
- 0052-mtd-spi-nor-use-4-bit-locking-for-MX25L12805D.patch
Fixes: 15aa53d7ee ("ath79: switch to Kernel 5.10")
Signed-off-by: Nick Hainke <vincent@systemli.org>
ipTIME A3004T is a 2.4/5GHz band router, based on Mediatek MT7621.
Specifications:
- SoC: MT7621 (880MHz)
- RAM: DDR3 256M
- Flash: NAND 128MB (Macronix NAND 128MiB 3,3V 8-bit)
- WiFi:
- 2.4GHz: MT7615E
- 5GHz : MT7615E
- Ethernet:
- 4x LAN
- 1x WAN
- USB: 1 * USB3.0 port
- UART:
- 3.3V, TX, RX, GND / 57600 8N1
Installation via web interface:
1. Flash initramfs image using OEM's Recovery mode
2. Boot into OpenWrt and perform sysupgrade with sysupgrade image.
Revert to stock firmware:
- Flash stock firmware via OEM's Recovery mode
How to use OEM's Recovery mode:
1. Power up with holding down the reset key until CPU LED stop blinking.
2. Set fixed ip with `192.168.0.2` with subnet mask `255.255.255.0`
3. Flash image via tftp to `192.168.0.1`
Additional Notes:
This router shares one MT7915E chip for both 2.4Ghz/5Ghz.
radio0 will not working on 5Ghz as it's not connected to the antenna.
Signed-off-by: WonJung Kim <git@won-jung.kim>
(added led dt-bindings)
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
WeVO AIR DUO is a 1-bay NAS & 802.11ac (Wi-Fi 5) router, based on
MediaTek MT7620A.
Specifications:
* SoC: MT7620A
* RAM: 64 MiB
* Flash: SPI NOR 16 MiB
* USB & SATA bridge controller: JMicron JMS567
* SATA 6Gb/s: 2.5" drive slot
* USB 3.0: Micro-B
* USB 2.0: connected to SoC
* Wi-Fi:
* 2.4 GHz: SoC built-in
* 5 GHz: MT7612EN
* Ethernet: 5x 1GbE
* Switch: MT7530WU
* UART: 4-pin 1.27 mm pitch through-hole (57600 baud)
* Pinout: (3V3)|(RXD) (TXD) (GND)
Notes:
* The drive is accessible through the external USB port only when the
router is turned off.
Installation via web interface:
1. Flash **initramfs** image through the stock web interface.
The image filename should have ".upload" extension.
2. Boot into OpenWrt and perform sysupgrade with sysupgrade image.
Revert to stock firmware:
1. Perform sysupgrade with stock image.
Signed-off-by: Sungbo Eo <mans0n@gorani.run>
According to the vendor [1] these HATs share the same DT overlay:
hifiberry-dacplus. The PCM512x-compatible control unit is attached to
I2C, so the additional snd-soc-pcm512x-i2c kernel module is required.
Also explicitly note the Amp2 support to reduce confusion for those
users.
[1] <https://www.hifiberry.com/docs/software/configuring-linux-3-18-x/>
Signed-off-by: Torsten Duwe <duwe@lst.de>
(added bcm27xx tag, changed commit message)
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
NETGEAR ReadyNAS Duo v2 is a NAS based on Marvell kirkwood SoC.
Specification:
- Processor Marvell 88F6282 (1.6 GHz)
- 256MB RAM
- 128MB NAND
- 1x GBE LAN port (PHY: Marvell 88E1318)
- 1x USB 2.0
- 2x USB 3.0
- 2x SATA
- 3x button
- 5x leds
- serial on J5 connector accessible from rear panel
(115200 8N1) (VCC,TX,RX,GND) (3V3 LOGIC!)
Installation by USB + serial:
- Copy initramfs image to fat32 usb drive
- Connect pendrive to USB 2.0 front socket
- Connect serial console
- Stop booting in u-boot
- Do:
usb reset
setenv bootargs 'console=ttyS0,115200n8 earlyprintk'
setenv bootcmd 'nand read.e 0x1200000 0x200000 0x600000;bootm 0x1200000'
saveenv
fatload usb 0:1 0x1200000 openwrt-kirkwood-netgear_readynas-duo-v2-initramfs-uImage
bootm 0x1200000
- copy sysupgrade image via ssh.
- run sysupgrade
Installation by TFTP + serial:
- Setup TFTP server and copy initramfs image
- Connect serial console
- Stop booting in u-boot
- Do:
setenv bootargs 'console=ttyS0,115200n8 earlyprintk'
setenv bootcmd 'nand read.e 0x1200000 0x200000 0x600000;bootm 0x1200000'
saveenv
setenv serverip 192.168.1.1
setenv ipaddr 192.168.1.2
tftpboot 0x1200000 openwrt-kirkwood-netgear_readynas-duo-v2-initramfs-uImage
bootm 0x1200000
- copy sysupgrade image via ssh.
- run sysupgrade
Known issues:
- Power button and PHY INTn pin are connected to the same GPIO. It
causes that every network restart button is pressed in system.
As workaround, button is used as regular BTN_1.
For more info please look at file:
RND_5.3.13_WW.src/u-boot/board/mv_feroceon/mv_hal/usibootup/usibootup.c
from Netgear GPL sources.
Tested-by: Raylynn Knight <rayknight@me.com>
Tested-by: Lech Perczak <lech.perczak@gmail.com>
Signed-off-by: Pawel Dembicki <paweldembicki@gmail.com>
Linkstation poweroff driver was added to mvebu target, but is required
for kirkwood target too.
This commit make two changes:
- move linkstation-poweroff support patch from mvebu to generic and
replace upstream accepted version
- backport small linkstation-poweroff fix from 5.12
Signed-off-by: Pawel Dembicki <paweldembicki@gmail.com>
The GPIO expander is connected via I2C, thus the can_sleep flag has to
be set to true. This should fix spurious "scheduling while atomic" bugs
in the kernel ringbuffer.
Signed-off-by: David Bauer <mail@david-bauer.net>
Upon comment of Russell King ('Oh no, not this "-1 disease" again.')
clean up mdio read and write return type and value in mtk_eth_soc
driver and also use appropriate return values for bus-busy-timeout-
errors in newly added Clause 45 access code.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Replace recently added patch
701-net-ethernet-mtk_eth_soc-add-support-for-clause-45-mdio.patch
with version sent upstream
701-net-ethernet-mtk_eth_soc-implement-Clause-45-MDIO-access.patch
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Copy and refresh patches and config from 5.4 to 5.10. Most patches
require no more then automatic refresh. The only exception is the
Ethernet driver patch, which requires some more work:
* drop eth_change_mtu() usage since it was removed from the kernel,
it anyway useless for drivers that utilizes alloc_etherdev();
* add the txqueue number argument to the .ndo_tx_timeout callback
function;
* replace ioremap_nocache() which was finally removed from the kernel by
the ioremap() with the same behaviour.
Switch target to the new kernel version.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
[use KERNEL_TESTING_PATCHVER for now]
Signed-off-by: Sergey Ryazanov <ryazanov.s.a@gmail.com>
The target config require some refresh due to the just introduced
filtering of the "run-time" options, MIPS eBPF JIT backporting, and so
on.
The configuration is easily updated using make kernel_oldconfig. So
let's update it now in preparation for v5.10 support to reduce the new
kernel configuration diff.
Signed-off-by: Sergey Ryazanov <ryazanov.s.a@gmail.com>
ath25 requires a 88E6060 driver to support boards such as Fonera 2.0g
(FON2202). The swconfig based mvswitch driver has not yet been ported to
the 5.10 kernel as the only user is the ath25 target while all other
targets have been switched to the upstream DSA implementation.
Switching ath25 to the DSA implementation is a complex task, since we
need either per-board platform data or DTS support. ath25 lacks both of
them and builds only a single generic image. So we need to keep the
swconfig driver implementation to easly and quickly port ath25 to the
5.10 kernel.
Since porting the mvswitch driver to 5.10 as a generic driver is not an
option, and since the ath25 is its only user, make mvswitch a target
specific driver to be able to port it to the 5.10 kernel as part of the
kernel version update of the target. This will allow us quickly migrate
to the next kernel version and not delay the next firmware release.
Suggested-by: Felix Fietkau <nbd@nbd.name>
Signed-off-by: Sergey Ryazanov <ryazanov.s.a@gmail.com>
These never worked and upstream is in the process of removing
them as well. Legacy PCI interrupt signaling is still working
as before.
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
Apart from the dtb partition, these were all "read-only;"
they serve no purpose other than being a copy of what
netgear had defined in their original firmware.
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
where to begin? the USB regulator settings were just
a part of the issue. With them changed, according to
the forum it still failed when a USB device was
connected to the port with:
dwc2 4bff80000.usbotg: dwc2_restore_global_registers: no global registers to restore
dwc2 4bff80000.usbotg: dwc2_exit_partial_power_down: failed to restore registers
dwc2 4bff80000.usbotg: exit partial_power_down failed
dwc2 4bff80000.usbotg: HC died; cleaning up
One clue was found upstream in
commit cc10ce0c51b1 ("usb: dwc2: disable power_down on Amlogic devices")
|Disable power_down by setting the parameter to
|DWC2_POWER_DOWN_PARAM_NONE. This fixes a problem on various Amlogic
|Meson SoCs where USB devices are only recognized when plugged in before
|booting Linux. A hot-plugged USB device was not detected even though the
|device got power (my USB thumb drive for example has an LED which lit
|up).
|[...]
the same method proposed there worked with APM821xx's USB IP-Core.
Link: https://forum.openwrt.org/t/wd-my-book-duo-usb/111926/2
Reported-by: thwe and takimata (openwrt forum)
Fixes: b70d3557e0 ("apm821xx: clean up gpio-hogs")
Signed-off-by: Christian Lamparter <chunkeey@gmail.com>
The GS110TPP has an RGB LED used for system status indication. Expose
all three components as separate GPIO LEDs connected via the device's
RTL8231.
Signed-off-by: Sander Vanheule <sander@svanheule.net>
Since the move to 5.10, there are now two GPIO drivers. The gpio0 node
refers to the internal GPIOs, so the indirect-access-bus-id is no longer
relevant for that node.
Set indirect-access-bus-id to the correct value (31) on the correct node
(gpio1) and enable the device.
Cc: Raylynn Knight <rayknight@me.com>
Cc: Michael Mohr <akihana@gmail.com>
Cc: Stijn Segers <foss@volatilesystems.org>
Cc: Stijn Tintel <stijn@linux-ipv6.be>
Signed-off-by: Sander Vanheule <sander@svanheule.net>
Tested-by: Bjørn Mork <bjorn@mork.no>
Assuming cmdlinepart is only one level deep partition scheme and that
static partition are also defined in DTS, we can assign an of_node for
partition declared from bootargs.
The cmdlinepart parser is the first parser checked and if it does find
some partition declared in the bootargs, every other parser is ignored.
This means that the fixed-partition parser is ignored and an of_node for
the mtd is never assigned.
Fix this by searching a defined of_node using a similar fixed_partition
parsing logig, check if a partition is present with the same label, check
that it has the same offset and size and finally assign an of_node to the
mtd. The NVMEM can now find the of_node for the mtd and correctly works.
Fixes: abc17bf306 ("ath79: convert mtd-mac-address to nvmem implementation")
Tested-by: Sven Eckelmann <sven@narfation.org>
Signed-off-by: Ansuel Smith <ansuelsmth@gmail.com>
The UBNT_REVISION was already added for the ubnt-xw target because:
U-boot bootloader on M-XW devices expects factory image revision
version in specific format. On airOS v6.1.7 with `U-Boot 1.1.4-s1039
(May 24 2017 - 15:58:18)` bootloader checks if the revision major(?)
number is actually a number, but in currently generated images there's
OpenWrt text and so the check fails
...
By placing arbitrary correct number first in major version, we make the
bootloader happy and we can flash factory images over TFTP again.
commit d42a7c4699 ("ath79: ubnt-m-xw: Fix factory image flashing using TFTP recovery method")
Fixes errors in the form of (tftp flashing):
sent DATA <block=8577, 412 bytes>
received ERROR <code=2, msg=Firmware check failed>
Error code 2: Firmware check failed
The missing UBNT_REVISION was not noticed before, since the
UBNT_REVISION field for the ubnt-xm target was also set to:
"42.OpenWrt-..."
Probably, UBNT_REVISION for the ubnt-xm target was set by the ubnt-xw
and was never overridden somewhere else. However, it is missing and
should be part of the ubnt-xm device.
Signed-off-by: Nick Hainke <vincent@systemli.org>
The firmware for the rtl8723bs chip is now included in the
rtl8723bu-firmware package.
Fixes: 397dfe4a97 ("linux-firmware: Update to version 20121216")
Signed-off-by: Hauke Mehrtens <hauke@hauke-m.de>
This change enables proper Ethernet link status and speed reporting on
the Ubiquiti UniFi 6 LR access point:
mtk_soc_eth 1b100000.ethernet eth0: PHY [mdio-bus:08] driver [Aquantia AQR112C] (irq=POLL)
mtk_soc_eth 1b100000.ethernet eth0: configuring for phy/2500base-x link mode
mtk_soc_eth 1b100000.ethernet eth0: Link is Up - 1Gbps/Full - flow control rx/tx
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Enable Aquantia Ethernet PHY driver as there is an AQR112C 2500Base-T
PHY in the Ubiquiti UniFi 6 LR access point.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Fix default network configuration of the Puzzle-M902 so all LAN ports
are included in the LAN bridge.
Setup network LED to indicate WAN port link status, like vendor
firmware does as well.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Fixes Ethernet link status on all ports and makes 2.5G ports usable
in 2.5G and 1G full-duplex mode.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Copy and refresh patch enabling AQR112 and AQR412 Ethernet PHY from
layerscape (5.4) target to generic (5.10) as AQR112 can also be found
on other targets as well.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Wire up MCU driver for LEDs, fan and temperature sensor, and add
GPIO reset button just like on the M902 also on the Puzzle M901.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Set blinking mode using scheduled work instead of blocking which may
result in deadlocks.
Add dynamic kprintf debugging hexdumps of all MCU rx and tx.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>
Kernel 5.10 is used by many people since quite a while. With other
targets already moved to 5.10, let ath79 follow suit.
Tested-by: Stefan Lippers-Hollmann <s.l-h@gmx.de> [ath79/tl-wdr3600; ath79/tl-wdr4300]
Tested-by: Aleksander Jan Bajkowski <olek2@wp.pl> [ath79/tl-wdr4300]
Signed-off-by: Paul Spooren <mail@aparcar.org>
Signed-off-by: David Bauer <mail@david-bauer.net>
This device is based on NXP's QorIQ T2081QDS board, with a quad-core
dual-threaded 1.5 GHz ppc64 CPU and 4GB ECC RAM. The board has 5
ethernet interfaces, of which 3 are connected to the ethernet ports on
the front panel. The other 2 are internally connected to a Marvell
88E6171 switch; the other 5 ports of this switch are also connected to
the ethernet ports on the front panel.
Installation: write the sdcard image to an SD card. Stock U-Boot will
not boot, wait for it to fail then run these commands:
setenv OpenWrt_fdt image-watchguard-firebox-m300.dtb
setenv OpenWrt_kernel watchguard_firebox-m300-kernel.bin
setenv wgBootSysA 'setenv bootargs root=/dev/mmcblk0p2 rw rootdelay=2 console=$consoledev,$baudrate fsl_dpaa_fman.fsl_fm_max_frm=1530; ext2load mmc 0:1 $fdtaddr $OpenWrt_fdt; ext2load mmc 0:1 $loadaddr $OpenWrt_kernel; bootm $loadaddr - $fdtaddr'
saveenv
reset
The default U-Boot boot entry will now boot OpenWrt from the SD card.
Signed-off-by: Stijn Tintel <stijn@linux-ipv6.be>
Acked-by: Rui Salvaterra <rsalvaterra@gmail.com>
Add a new target named "qoriq", that will support boards using PowerPC
processors from NXP's QorIQ brand.
This doesn't actually add support for any board yet, so that
installation instructions can go in the commit message of the commit
that adds actual support for a board.
Using CONFIG_E6500_CPU here due to the kernel using -mcpu=powerpc64
rather than -mcpu=e5500 when selecting CONFIG_E5500_CPU. The only
difference between e5500 and e6500 is AltiVec support, and the kernel
checks for it at runtime. Musl will only check at runtime if AltiVec
support is disabled at compile-time, so we need to use e5500 in CPU_TYPE
to avoid SIGILL.
Math emulation (CONFIG_MATH_EMULATION_HW_UNIMPLEMENTED) is required, as
neither e5500 nor e6500 implement fsqrt nor fsqrts, and musl hardcodes
sqrt and sqrtf to use these ASM instructions on PowerPC64.
Signed-off-by: Stijn Tintel <stijn@linux-ipv6.be>
Reviewed-by: Rui Salvaterra <rsalvaterra@gmail.com>
Backport MFD driver for communicating with the on-board MCU found on
IEI World Puzzle appliances.
Improve the driver to support multiple LEDs, apply a default state and
let MCU take care of blinking if timing is within supported range.
Wire up LEDs and fan for Puzzle M902 in device tree.
Signed-off-by: Daniel Golle <daniel@makrotopia.org>